More 1959 Austin Healey 3000 repairs

More 1959 Austin Healey 3000 repairs

Jonn secured all track rod ends on our 1959 Austin Healey 3000 and tightened the ball joint before fitting a new split pin. With the steering components addressed, he lowered the car to the floor and confirmed that the tracking remained correctly set, with plans to check it again following a road test. He then […]

500SL Door Glass

Jonn carried out work on the passenger’s door window of our 1987 Mercedes 500SL. He located the glass and the rear section runner, but as the original fixings could not be found at the time, he cut down two 6mm bolts to use in their place. The channel was fitted and greased to ensure smooth […]

More Morgan Repairs

Jonn carefully applied heat to the steering wheel of our Morgan 4/4 in order to remove it. Once removed, he turned the wheel to the left and refitted it to correct the alignment. An initial test was carried out around the yard, followed by a run up the road, both confirming that the steering wheel […]

Rover Vitesse Inspection

Jonn brought the Rover Vitesse into the workshop and jacked up the vehicle to remove the front wheels. On the offside, he stripped out the track rod end, which was found to be seized in place. To resolve this, he cut off the track rod end and removed it, then applied heat to the track […]

Austin Devon Kick Boards

Kickboards have been made and fitted. to our 1951 Austin Devon Pickup.

Seat Repair

A new elastic seat web base has been fitted to our Morgan. The old one had completely perished and collapsed, so a new one was needed.

Morgan 4/4 Repairs

Jonn hoovered out the interior of our 1984 Morgan 4/4 before refitting the driver’s seat. To ensure the seat was securely installed and to distribute the load more evenly, repair washers were fitted beneath the floor. He then removed the gear lever to investigate further issues, during which he found remnants of a broken bush. […]

Porsche 911 Backplate

Jonn investigated a rattle coming from the offside rear of our 2007 Porsche 911 and identified the backplate as the source. He removed the wheel and calliper, then de-adjusted the handbrake shoes to allow for the removal of the disc. With the disc off, he cleaned the handbrake shoes and inspected the dust shield, which […]

Rover Vitesse Column bush

Jonn has addressed an issue with the steering column lower bush on our 1987 Rover Vitesse. He began by undoing the securing plate at the bulkhead, then proceeded to clean the splines on the steering shaft and slacken the universal joint. The shaft was knocked down, and alignment marks were made on the splines to […]

Jensen Interceptor Interior pieces

Some interior pieces can finally be fitted to our 1976 Jensen Interceptor without being in anyone else’s way. Carpet side pieces are in, and under-seat runners are covered in vinyl.

Aston Martin DB2/4 Boot Lid

The boot lid has been refitted to our 1955 Aston Martin DB2/4 Drophead Coupe.

Suspension And Underside

Ben has been assembling various components for the suspension, cleaning threads and fitting bushings on our 1969 Aston Martin DB6 Volante. He built up the new koni shock absorbers and started fitting, but further checks showed these should be black, even though our Aston Martin parts company supplied red units. So these were removed and […]

New Cylinders

The rear brake wheel cylinders were corroded and leaking on our 1966 Volvo Amazon, so they were replaced along with the O/S metal brake pipe, as it was seized in the old cylinder.

Battery Replacement

The old battery was removed from our 1947 Wolseley Eight. The new battery came dry, so had acid added and the battery was charged.

Engine Bay Prep And Paint

The engine bay of our 1967 MGB Roadster has been prepped, had epoxy primer applied before being painted.

Mercedes 350SL Boot Floor

The spare wheel well and boot floor have been prepped and welded in on our 1978 Mercedes 350SL. Spot welding was completed in factory spots and dressed back. Towing eye fabricated and welded in factory position. Preparation for further panel work.

Repairs On Our Healey

Jonn has been working on our 1959 Austin Healey 3000 by removing both carburettors from the engine. Each unit was then stripped down, thoroughly cleaned, and blown out to remove any residual debris or buildup. Following this, the carburettors were carefully rebuilt with attention to detail, ensuring all components were correctly reassembled. Lubrication was applied […]

More DB6 Progress

The rack mounts and parts of our 1969 Aston Martin DB6 Volante, which Ben anodised, like the shims that set the suspension geometry, are seen in the pictures below. The new bering races have been pressed into the hubs and then a coat of paint after masking up otherwise the paint would likely have been […]

Ford Thunderbird Repairs

Jonn has been looking at our 2002 Ford Thunderbird, beginning with pressing the front lower ball joints into the hubs. He then refitted the back plates and bolted the hubs into place before installing the brake discs and new pads. The ABS sensors were refitted, and the wheels were mounted before lowering the vehicle to […]

Austin Healey Repairs

Jonn carried out work on our 1959 Austin Healey 3000, beginning with the installation of a new offside front wheel bearing. He fully greased and adjusted the bearing, then refitted the wheel and conducted an initial test. After removing the wheel to readjust the bearing, he refitted and tested it again, confirming it was operating […]

Austin Devon Wheel Arch

The wheel arch of our 1951 Austin Devon has been painted ready to go back onto the car.

Painting An Austin Healey 3000

Our 1959 Austin Healey 3000 has been getting some attention in the Bridge Classic Cars paint shop.

Wolseley Eight – Starter Motor

Pete inspected the starting issues on our 1947 Wolseley Eight, beginning with the battery, where he found the terminals to be in poor condition. The positive post was lifting from the battery case when attempting to remove the clamp, so the system was isolated via the earth strap to prevent any electrical faults. He then […]

Boot Rework

Both colours needed reworking on the inner boot lip of our 1973 MGB Roadster.

New caps

The caps on both fill points have been changed on our 1989 Daimler Double Six. The coolant level was checked and the car was road tested for a final time. The car behaves exactly as expected

Post Acid Dip Appraisal

Today Pete has brought the body into our workshop and removed it from its transport trolly, it’s been safely put onto our two poster ramp ready for fabrication work to start. In the meantime Pete and our photographer Nick have taken a wealth of photos of all the areas we can access that need repair […]

Radiator Brackets

Work has begun on aligning the radiator brackets and working out how both radiators fit on our 1987 Maserati BiTurbo..

Oil leak And New Parts

The fuel pump that sits on the side of the engine of our 1977 Alfa Romeo 2000 was leaking oil from the old gaskets, so new gaskets were made and fitted. The old seat belts had some staining on them that couldn’t be removed, so they were replaced with nice clean new ones, and the […]

More Repairs

Jonn continued repairs on our 1997 Mercedes 280SL by inspecting the offside front fog light. He confirmed the bulb was intact and the fuses were in working order. After cleaning the connector, the light functioned correctly, and he then refitted the arch liner. Moving to the centre air vents, he removed and stripped them, reattaching […]

MGB Roadster – New hood

The old vinyl hood was removed from our 1979 MGB Roadster. It was replaced with a new double-duck canvas type one instead.