As part of its pre-delivery inspection, we’ve carried out a thorough service and our technician Paul is currently addressing the issues that have arisen from the service. There was a noise at the rear end caused by worn brake pads which were rubbing metal to metal on the brake disk. One brake was cracked as […]
We’ve been working on the engine for this MG B V8 and now the rest of the car has finally come in for us to fit the engine.
The gearbox has been crunching in our 1965 Amphicar so we’ve removed it to try and address the issues with the syncro-mesh when changing down gears.
Our 1989 Jaguar XJS that has recently been finished is currently undergoing a pre-delivery inspection during which we’ve discovered it needs new brakes.
We’ve got this fantastic 1957 3600 Chevrolet Truck in for a new clutch however we’re currently waiting on the parts to arrive. So until then, its on show sat on the ramp.
Mauro has been working on our 1973 Bristol which has had its exhaust manifold refacing due to leaking. He’s also added new spark plugs.
Our Fiat 500 has passed in MOT with flying colours and has now been completed and awaiting collection. We’re delighted to see this little Italian Fiat back on the road.
John recently completed the work on our Triumph Dolomite as the wheel cylinders were leaking and ceased, he replaced the dynamo, and then took apart the brakes to be refurbished.
Brian has been working on adding headrest brackets onto the seats by adding the chrome trim. He’s stapled the bottom of the frame, cut holes for the brakes and fitted them. The fabrication bay have also completed stripping the body to bare metal so that its now ready for paint prep. Chris has begun coating […]
Our lovely 1971 Range Rover Classic has come back in after a breakdown due to an issue with the starter motor. John, our head technician has been working on trying to understand the issue. He’s set to replace the starter motor fitted due to a failure of the old starter motor solenoid not engaging. It […]
Scott has begun to take apart the brakes on our 1934 Riley Monaco to determine the issue. He’s stripped the brakes down and checked them over, cleaned and greased them. He discovered that they still squeaked, so he filed the leading edge of the shoes to a chamfered edge. Unfortunately, Scott found that the squeaking […]
This 1934 Riley Monaco has come in to address the squeaking brakes, which are making rather severe noises. We’ll start taking them apart to see what the issue is.
We did an impromptu live at Helmingham Hall where we gave our viewers another peak at our 1989 Jaguar XJS and 1996 Mercedes CL 500 which were won just a few days later by two lucky winners. Helmingham hall set as the perfect backdrop to our video and gave us the chance to not only […]
Our 1968 Triumph TR5 is on the home straight with just a handful of fine tuning tweaks that need to be carried out. We’ve noticed a few small running issues and exhaust troubles that we will address next.
Our 1965 Amphicar had a dip in the pool to test its seals against the water. The result was small ingress of water and we’ve discovered that a few small holes we’d filled in thinking they were holes, actually happen to be integral to the water flow and buoyancy of the Amphicar as they allow […]
Ady has been stripping the carbs down on our MGB V8 so that he can inspect, clean and put them back together.
Our 1973 Bristol 411 Series 3 is in for a service and a dent repair. Mauro has been working on fixing the door which is hard to open. This has meant Mauro has had to adjust the rod and linkage. He is also replacing the window seal. We’ve sent the exhaust manifold off to be […]
After engine rebuild, our MG was taken to the owners boat for a day out with his grandchildren, both had a ride in the MG, all happy.
Our 1960 Jensen 541S has had new chrome fitted around the door as well as ‘weather strips’. Paul has been working to apply the smaller chrome details. Paul has also fitted a new dynamometer.
We’re on the home straight with the steering correction on our 1969 Fiat 500 Abarth. The new column is now in with new bearings and strengthening plate. We’ve modified the existing shaft to facilitate a new one. We’ve then patched up the holes. The steering has changed from a box to a rack during this […]
We’ve made some more modifications to our 1969 Fiat 500. The demister diverter heater control for the floor and windscreen has been modified and moved to accommodate the new steering rack.
We’ve started repainting the floor on our 1965 Amphicar. Chris began by taking out the bolts and masking up the struts that would remain cream. We’ve applied a black sealant paint on the inside which is the same as the underside. This resin based paint provides better protection against water ingress and allows for easier […]
With only 183 ever made, this little HMC is both rare and collectable. Finished in a stunning blue, this classic bears a strong resemblance to Austin Healey. HMC (Holmes Motor Company) was founded in 1984 by two brothers, Graham and Peter Holmes who were inspired by the beautiful shapes of Austin Healeys. However, due to […]
Craig’s DB9 is currently in the paint shop undergoing some paint corrections after the epoxy primer was applied to treat a small amount of corrosion coming through around the door handles. We’ve also fitted new door rubber and rear window rubber tightened up the rear centre mounted brake lights that were rattling, refurbish the tyres, […]
Scott has continued the disassembly of our 1955 Aston Martin DB2/4 Mark I by taking apart the mechanics piece by piece so we can access the engine. Scott has also been removing some more of the wiring loom and then the the engine.
After the client came to see his two Jensen’s, he’s asked for some small modifications which has included changing the yellow Jensen badge to blue, adding mesh grills into the front side vents and we’ve noticed a few places where we wanted to touch up the paint. This Jensen will be leaving us very soon […]
We’ve bene waiting on the parts for our 1969 Fiat 500 Abarth for many months as they were stuck abroad due to a shipping error. Now, finally with us, we can get started with replacing and modifying the steering rack.
Our 1959 Ford Anglia has been polished and is now being inspected as part of its service. We’re replacing the oil cylinder as we found a leak. We’re also replacing the fuel pump and need to take it for a test drive. Lydia has also been making a new boot carpet for our Ford. She […]
Our 1973 Triumph Stag is looking worlds away from what it did when it came to us just a few months ago. We’ve sent off the steering rack which is being overhauled due to a leak and the rear brake shoes and brake flexihoses are being replaced. After this it will just need to be […]
Scott has been stripping down our 1955 Aston Martin DB2/4 in preparation for bodywork. This has involved taking out chrome, door cards, electrics and mechanics, all the interior and wiring.