John refitted the driver’s carpet on our 1972 Triumph Stag as neatly as possible. The roof catches were repaired to eliminate free play and subsequently adjusted for proper engagement. He also repositioned the door sticker to achieve a better fit. The movement in the roof catches was addressed as part of the adjustments.
John refitted the exhaust on our 1972 Triumph Stag following its repair, using new rubbers to secure it in place.
Jonn continued work on our 1959 Austin Healey 3000 with the arrival of the throttle bar bushes. He used trimmed P-clips to secure the new bushes within the existing brackets and determined the most effective method for mounting before proceeding with fitting them back onto the car. The rod position on the end of the […]
Tony packed up our 1968 Austin Mini Cooper S to be delivered to the lucky winner Derek Brooks.
Lydia has been carefully fitting carpets for our 1976 Jensen Interceptor.
Greg removed the old corroded battery tray from our 1993 Ford Escort XR3i Silver and replaced it with a bespoke fabricated unit. He then applied paint protection and sealed the area to ensure durability and resistance to future corrosion.
Jonn fitted a new manifold-to-downpipe gasket on our 1984 Morgan 4/4, ensuring it was properly sealed and securely fastened. A new starter motor was sourced, but it proved to be the incorrect type.
Ben worked on our 1976 Jensen Interceptor by scraping down the underside in preparation for protective coating, working alongside Greg to mask off the suspension and paintwork. He then sprayed the underside with 3M underseal, taking care to touch in any hard-to-reach areas for full coverage. The rear springs were also prepped for finishing, with […]
Jonn investigated an exhaust blow on our 1984 Morgan 4/4, traced to the joint between the manifold and downpipe. He applied heat to release and remove the downpipe nuts and studs, then cleaned both mating surfaces as thoroughly as possible given the limited access. The starter motor was removed in preparation for fitting a new […]
John traced a fault in the wiring on our 1978 MG Midget 1500 and identified a section of melted wiring as the source of the issue. He removed the damaged wiring and installed a replacement to restore proper electrical function. Jonn brought our 1978 MG Midget out from the Classic Lounge and conducted a road […]
Greg carried out cleaning work on our 1976 Jensen Interceptor, focusing on the wheel arches and removing the existing undercoat. This preparation is essential ahead of applying a fresh layer of undercoat to ensure proper adhesion and protection.
Mauro applied epoxy primer to the floor panels and gearbox tunnel of our 1953 Aston Martin DB2/4, followed by a coat of direct-to-metal satin black paint to provide a durable and protective finish.
We’ve had a whole host of new arrivals over the past week or so! From old to brand new, the team always look forward to welcoming any car to our Pettistree workshops. 1988 Volkswagen Golf GTi: 1995 TVR Chimaera: 2003 Porsche Boxster: 2004 Alpina Roadster S: 2007 Range Rover: 2014 Range Rover Sport: 2024 Lotus […]
Ben continued work on our 1976 Jensen Interceptor by fitting the hood stay and making adjustments to the dampers. He cleaned and polished the washer jets to improve their appearance and functionality, and cut new rubber gaskets for the wiper chrome bezels. With these components prepared, he proceeded with fitting the new parts in place.
Pete removed the rear H-frame from our 1978 Mercedes 350SL and began trimming back to the chassis tail ends in preparation for fitting the new rear crossmember, which will be tied into the replacement boot floor. Despite the location being deep behind the bodywork, corrosion was still present in these areas. Fortunately, the acid dip […]
Lydia has fitted a brand new set of green carpets in the Austin Devon Pickup.
Jonn secured all track rod ends on our 1959 Austin Healey 3000 and tightened the ball joint before fitting a new split pin. With the steering components addressed, he lowered the car to the floor and confirmed that the tracking remained correctly set, with plans to check it again following a road test. He then […]
Jonn carefully applied heat to the steering wheel of our Morgan 4/4 in order to remove it. Once removed, he turned the wheel to the left and refitted it to correct the alignment. An initial test was carried out around the yard, followed by a run up the road, both confirming that the steering wheel […]
Jonn brought the Rover Vitesse into the workshop and jacked up the vehicle to remove the front wheels. On the offside, he stripped out the track rod end, which was found to be seized in place. To resolve this, he cut off the track rod end and removed it, then applied heat to the track […]
Kickboards have been made and fitted. to our 1951 Austin Devon Pickup.
Jonn hoovered out the interior of our 1984 Morgan 4/4 before refitting the driver’s seat. To ensure the seat was securely installed and to distribute the load more evenly, repair washers were fitted beneath the floor. He then removed the gear lever to investigate further issues, during which he found remnants of a broken bush. […]
Jonn investigated a rattle coming from the offside rear of our 2007 Porsche 911 and identified the backplate as the source. He removed the wheel and calliper, then de-adjusted the handbrake shoes to allow for the removal of the disc. With the disc off, he cleaned the handbrake shoes and inspected the dust shield, which […]
Jonn has addressed an issue with the steering column lower bush on our 1987 Rover Vitesse. He began by undoing the securing plate at the bulkhead, then proceeded to clean the splines on the steering shaft and slacken the universal joint. The shaft was knocked down, and alignment marks were made on the splines to […]
Some interior pieces can finally be fitted to our 1976 Jensen Interceptor without being in anyone else’s way. Carpet side pieces are in, and under-seat runners are covered in vinyl.
The boot lid has been refitted to our 1955 Aston Martin DB2/4 Drophead Coupe.
The rear brake wheel cylinders were corroded and leaking on our 1966 Volvo Amazon, so they were replaced along with the O/S metal brake pipe, as it was seized in the old cylinder.
The engine bay of our 1967 MGB Roadster has been prepped, had epoxy primer applied before being painted.
The spare wheel well and boot floor have been prepped and welded in on our 1978 Mercedes 350SL. Spot welding was completed in factory spots and dressed back. Towing eye fabricated and welded in factory position. Preparation for further panel work.
Jonn has been working on our 1959 Austin Healey 3000 by removing both carburettors from the engine. Each unit was then stripped down, thoroughly cleaned, and blown out to remove any residual debris or buildup. Following this, the carburettors were carefully rebuilt with attention to detail, ensuring all components were correctly reassembled. Lubrication was applied […]
Jonn carried out work on our 1959 Austin Healey 3000, beginning with the installation of a new offside front wheel bearing. He fully greased and adjusted the bearing, then refitted the wheel and conducted an initial test. After removing the wheel to readjust the bearing, he refitted and tested it again, confirming it was operating […]